Big Ugly Bug (BUB)
This project was my second attempt to scratch-build a model rocket with
available materials. I decided early in the project that I would try
not to use any materials made expressly for building rockets. This
was to keep costs down and give me some bragging rights among the other
rocket club members.
After the success of the
Ugly Bug, I wanted to stick to the
Estes Mosquito
design plan. Despite it's rather unpleasing proportions, I like the
design. I built (and lost) many Mosquitoes in my youth, since they were
the smallest and cheapest kit you could buy. I also liked the fact that
they were almost all engine, and were therefore a 'muscle-rocket' design
despite their diminutive size.
The first component I found for the BUB was a spiral-wound cardboard mailing
tube. This was about 3" in diameter. I located pictures and plans for the
original Mosquito on both the
Estes/Cox
and JimZ Rocket Plans
websites. From
these images I measured the rocket specs as well as I could, and obtained
approximate aspect ratio and fin dimensions. I cut the tube to the proper
length and was on my way.
The fins were an area I did the most thinking on. The
Ugly Bug had done very
well with fins made from brown paper, soaked with glue, laminated over corrugated
cardboard. I didn't feel the material was strong enough for the scaled-up
design, however. The Mosquito has very long fins compared to the root edge
length, and therefore can't depend on the glue joint to keep them stiff. I
decided to use a lamination of fiberglass over a corrugated cardboard core
for both strength and cheapness. I bought some cut-strand-mat fiberglass
cloth and resin from
Wal-Mart, and located a sturdy cardboard box to cut
cores from.
To serve as a sort of primitive mold, I used two sheets of glass coated with car
wax. I cut the mat to fit the cores, mixed the resin, painted a coat on to the
core, applied the mats (one per side), and another coat of resin to saturate it. This was
then placed on one sheet of glass, and the other sheet placed on top to sandwich
the fin in between. Some heavy books helped keep the fin squeezed between the
glass sheets. This eliminates air bubbles and keeps the fin straight.
When you work with fiberglass, you should wear gloves to keep the cut ends
from getting on your skin. The resin is also super-gooey and difficult to
remove from fingers. Some cheap PVC painters gloves work very well. By the
way, the resin also really stinks, so be aware of that when choosing a
place to work with fiberglass. For more info on fabricating fiberglass parts,
check out Bryan Feldman's
site. It refers to carbon fiber cloth, but fiberglass layup is identical.
After about half an hour the resin had cured enough to remove the weights
and gently pry the glass sheets away from the fin. The fin was then set
aside to dry and cure fully while I built the next one. Three were required
for the BUB. After each fin cured, I sanded the edges with a belt sander. The
corrugated edges were plugged up with
Bondo auto body filler, which is
chemically very similar to the fiberglass resin, but has talcum powder added
to give a paste-like consistency. The filler was added to all edges except the
root, where the fin would attach to the rocket body. After curing, the
filler was sanded to a rounded shape. The fins were then set aside to dry fully.
To build the motor mount, I first decided on the size of motor I wanted to
use. The 24mm
Estes 'D' casing was my choice.
Later, when the BUB turned
out heavier than I had expected, I ended up using an
Aerotech 24mm reloadable
composite motor. This could be loaded with kits with either E or F power
ranges, enough to lift the rocket safely. Anyway, I cut more brown paper
bags in to strips, soaked them in glue, and wrapped them on an dowel that
was 24mm in diameter and had been wrapped in plastic to keep it from
sticking. I removed the dowel, let the tube dry, and cut it to length
(the length of a D motor plus about an inch). For a motor retention hook,
I used a steel street sweeper bristle I found in a gutter. This was cleaned
with steel wool, cut to length, and bent to form the hook. For a thrust
block, I used a chunk of the same dowel I had used as a form to build the
tube on. I drilled a hole in this to allow the ejection charge gasses to
escape. I mounted the hook and block in the motor mount so that a D casing
would extend about 3/4" from the bottom. The hook was strapped to the
tube with another wrap of glue-soaked paper, and the block simply glued in.
To mount this assembly, I measured and cut centering rings from the same
cardboard I had used for the fin cores. This was a bit tedious but worked
well enough. When everything fit, I glued the motor mount to the rings,
and when this was dry, glued the rings in the end of the body tube. The
BUB was starting to take shape!
After the motor mount was dry, I lightly sanded the body tube to remove the
shiny coating, so the adhesive would stick properly. I marked the tube
for a three-fin configuration and epoxied the fins in place. I used a
paste-like marine-rated epoxy that allowed me to make fillets at the fin
roots. The launch lug was a plastic soda straw, which was laminated into
one fillet for strength.
It was now time to build the nose. Not wanting to wimp out and buy one that
would fit (which would have been very difficult anyway since the Mosquito uses a
blunt, nearly hemispherical nose), I decided to turn one out of white
foam. A friend donated some foam packing blocks, which I glued together and
mounted on a hardwood dowel. This dowel I put in the chuck of a drillpress,
and I used a combination of files and sandpaper to shape the foam to the correct
form. This works well, but really makes a mess! To make the section of the nose
that slides into the body tube stronger, I used a section of body tube cut from
the spare piece and trimmed a section out of it so it would fit inside the body.
This I glued over the foam shank of the nose. I applied a protective layer of
wood glue to the entire nose, then put more
Bondo over the exterior section (the
resin in
Bondo
will dissolve white foam without the glue layer). Some sanding
and I had a nice, smooth nose, ready for painting. To finish off, I cut the
exposed part of the dowel off, drilled a pilot hole, and installed a screw-eye
for parachute attachment.
With all major parts done, it was time to paint. Like the UB, I decided to
paint the BUB blaze orange. The bigger rocket didn't really need it, but I
figured I had to go with tradition.
I mounted a long shock cord made from cotton clothesline rope, and a parachute
cut from garbage bag material completed the rocket. I now popped it on the scale
and discovered it weighed nearly a pound (16 oz)! The
Estes D wouldn't do for
that. Now was the time I decided to use the
Aerotech composite 24mm reload.
When I bought the motor, I discovered that it wouldn't fit: the ejection charge
tube was too big to go through the hole in the thrust block. With no way to
remove the mount from the rocket, I used a rat-tail file (and lots of curse-words)
to enlarge the hole in the block until the casing would fit.

The Big Ugly Bug at an
NDRA building session
The BUB was ready for its first flight in July of 2001. It would be my
first composite motor launch, as well as my first high-power rocket. Others
double-checked the balance point on the model with the motor in place to be sure it
would be reasonably stable in flight. Even so I was nervous and said a silent
prayer as the Range Safety Officer (RSO) counted down. At zero, I pressed the button
on the
Aerotech
controller, and the motor lit! The BUB came off the launch rod
at a slight angle, but still well within safe limits, and hissed skyward. The
four-second delay I chose was perfect: the rocket was just turning over at
about 500 feet when we heard the ejection charge pop. Unfortunately, the nose
stayed firmly on the rocket! All I could think was, "Oh No!" as the model
turned over and began its death-dive to the ground. The RSO shouted "Heads-Up!"
on the PA system over and over as the BUB executed a perfect ballistic dive
towards the parking area. With a resounding SPLAT the rocket hit the ground,
shattered its nose, and all three fins tore off and bounced several feet in the
air. As the kids present charged for the crash site, the RSO shouted at them not
to touch anything. I arrived at the site to see it was hopeless: the rocket was
a total loss. The fins were ok, but the nose and body tube were crushed beyond
any hope of repair. I was also not happy to see that my expensive 24mm motor
casing was gone. The retention hook had failed and the motor had ejected.
Luckily one of the other club members found it sitting in the grass near bye.
Disappointed as I was about the crash, I still laughed with amusement and relief
that everyone was safe and my first high-power rocket was mostly a success.
The crowd gave me a standing ovation for the most spectacular crash they had
seen, and others teased me about using the original Mosquito motor-ejection and
featherweight recovery system on the BUB.
This episode hasn't soured me on scratch-builts nor the Mosquito design. In
fact, I started work on the
Big Ugly Bug II in the winter of 2001. Instead of
'junkyard' parts, this one is incorporating bought parts like body tubes, motor
mount, thrust rings, parachute, and launch lug. I will still have to fabricate
the fins and nose, but the store-bought parts will help things go together more
quickly. And yes, this time I'm using a commercial motor retainer system, so
hopefully the parachute will come out!